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タイトルSCATHA mission termination report
本文(外部サイト)http://hdl.handle.net/2060/19930015536
著者(英)Stakkestad, Kjell; Fennessey, Richard
著者所属(英)Lockheed Technical Operations Co.|Consolidated Space Test Center
発行日1993-02-01
言語eng
内容記述The SCATHA (Spacecraft Charging at High Altitudes) satellite was operated from the Consolidated Space Test Center in Sunnyvale, California from February 1979 to May 1991. It was a spin stabilized vehicle in a highly eccentric orbit that collected data on spacecraft charging. The purpose of such data gathering was to predict and/or model the effects of the Earth's magnetic field on synchronous and near synchronous satellites. During the majority of its lifetime, attitude precession maneuvers were done every 10-15 days to maintain solar panel orientation. Maneuver planning was difficult due to the structural characteristics of SCATHA. It is cylindrically shaped and has seven booms ranging in length from 2 to 50 meters. These precession maneuvers induced predictable nutation that damped out after a few days. Eventually fuel began running low due to these frequent maneuvers. Experiments that had required the spin axis be in the orbit plane had already been turned off or had collected all their data. To increase the vehicle lifetime, the spin axis was moved to ecliptic normal. While this stopped the need for frequent attitude maneuvering (only two per year required now), this movement of the spin axis caused nutation that would not damp out for the remainder of the mission. This phase of the mission, with the ecliptic normal orientation, lasted for approximately three years. Although nutation never damped, data gathering was uninterrupted. In late 1990, when SCATHA's transmitter became seriously degraded, the Air Force decided to turn SCATHA off. This would only be done after the satellite was made 'safe'. The most difficult part of making the vehicle safe was quickly purging the fuel. Several plans were considered. The selected plan was to perform a series of 20 degree attitude precession maneuvers (3 days apart to allow for the worst nutation to damp) until the fuel was depleted. Although this sounded simple, the actual execution proved difficult. This was due to a nearly complete lack of available telemetry data, large undamped motion of the long booms, inadequacies in attitude determination software, and an error in the fuel level calculation software. This paper discusses the various proposed termination plans and execution of the selected one. Attitude determination methodologies, nutation from maneuvers, and effects of the flexible booms on the termination mission are presented and analyzed from a satellite analyst point of view.
NASA分類SPACECRAFT DESIGN, TESTING AND PERFORMANCE
レポートNO93N24725
権利Copyright, Distribution as joint owner in the copyright
URIhttps://repository.exst.jaxa.jp/dspace/handle/a-is/122318


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