JAXA Repository / AIREX 未来へ続く、宙(そら)への英知

このアイテムに関連するファイルはありません。

タイトルTest Results of the Modified Space Shuttle Main Engine at the Marshall Space Flight Center Technology Test Bed Facility
本文(外部サイト)http://hdl.handle.net/2060/19910014930
著者(英)Ise, M.; Dumbacher, D.; Singer, C.; Cook, J.
著者所属(英)NASA Marshall Space Flight Center
発行日1990-10-01
言語eng
内容記述A modified space shuttle main engine (SSME), which primarily includes an enlarged throat main combustion chamber with the acoustic cavities removed and a main injector with the stability control baffles removed, was tested. This one-of-a-kind engine's design changes are being evaluated for potential incorporation in the shuttle flight program in the mid-1990's. Engine testing was initiated on September 15, 1988 and has accumulated 1,915 seconds and 19 starts. Testing is being conducted to characterize the engine system performance, combustion stability with the baffle-less injector, and both low pressure oxidizer turbopump (LPOTP) and high pressure oxidizer turbopump (HPOTP) for suction performance. These test results are summarized and compared with the SSME flight configuration data base. Testing of this new generation SSME is the first product from the technology test bed (TTB). Figure test plans for the TTB include the highly instrumented flight configuration SSME and advanced liquid propulsion technology items.
NASA分類SPACECRAFT PROPULSION AND POWER
レポートNO91N24243
権利No Copyright
URIhttps://repository.exst.jaxa.jp/dspace/handle/a-is/132400


このリポジトリに保管されているアイテムは、他に指定されている場合を除き、著作権により保護されています。