タイトル | Test Results of the Modified Space Shuttle Main Engine at the Marshall Space Flight Center Technology Test Bed Facility |
本文(外部サイト) | http://hdl.handle.net/2060/19910014930 |
著者(英) | Ise, M.; Dumbacher, D.; Singer, C.; Cook, J. |
著者所属(英) | NASA Marshall Space Flight Center |
発行日 | 1990-10-01 |
言語 | eng |
内容記述 | A modified space shuttle main engine (SSME), which primarily includes an enlarged throat main combustion chamber with the acoustic cavities removed and a main injector with the stability control baffles removed, was tested. This one-of-a-kind engine's design changes are being evaluated for potential incorporation in the shuttle flight program in the mid-1990's. Engine testing was initiated on September 15, 1988 and has accumulated 1,915 seconds and 19 starts. Testing is being conducted to characterize the engine system performance, combustion stability with the baffle-less injector, and both low pressure oxidizer turbopump (LPOTP) and high pressure oxidizer turbopump (HPOTP) for suction performance. These test results are summarized and compared with the SSME flight configuration data base. Testing of this new generation SSME is the first product from the technology test bed (TTB). Figure test plans for the TTB include the highly instrumented flight configuration SSME and advanced liquid propulsion technology items. |
NASA分類 | SPACECRAFT PROPULSION AND POWER |
レポートNO | 91N24243 |
権利 | No Copyright |
URI | https://repository.exst.jaxa.jp/dspace/handle/a-is/132400 |