JAXA Repository / AIREX 未来へ続く、宙(そら)への英知

このアイテムに関連するファイルはありません。

タイトルAn investigation of the increase in vortex induced rolling moment associated with landing gear wake
本文(外部サイト)http://hdl.handle.net/2060/19760003950
著者(英)Patterson, J. C., Jr.; Jordan, F. L., Jr.
著者所属(英)NASA Langley Research Center
発行日1975-11-01
言語eng
内容記述Flight tests were conducted to verify the results found in ground base facilities of the effect of span lift load variation as well as the vortex attentuation of the high energy jet engine exhaust through proper thrust programming. During these flight tests a large increase in vortex strength was experienced as a result of extending the landing gear. Tests in the Langley Vortex Research Facility indicate that the wake produced by the landing gear may possibly form an aerodynamic endplate or reflection plane at the inboard edge of each inboard flap which increases the effective aspect ratio of the flap and thereby increases the strength of the flap outer edge vortex.
NASA分類AERODYNAMICS
レポートNO76N11038
NASA-TM-X-72786
権利No Copyright
URIhttps://repository.exst.jaxa.jp/dspace/handle/a-is/188170


このリポジトリに保管されているアイテムは、他に指定されている場合を除き、著作権により保護されています。