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タイトルChilldown study of the single stage inducer test rig
本文(外部サイト)http://hdl.handle.net/2060/19730015551
著者(英)Kimura, L. A.
著者所属(英)Aerojet Nuclear Systems Co.
発行日1972-06-02
言語eng
内容記述Of the six chilldown tests, data from only one could be used for evaluation. During the rest of the chilldown tests, there was leakage hydrogen flow into the pump cavity prior to the initiation of the chilldown test. In all of the tests the hydrogen condition into the pump was probably 100% vapor. The data from this one test, therefore, can be used to compare only the single phase fluid correlation in the analytical pump chilldown model. In general, the actual pump chilled down much faster than predicted by the analytical pump model. There were insufficient data from the test to measure the pump flow rate and pump inlet fluid condition; therefore, these parameters were extrapolated based on related data which were available. However, even with the highest probable flow rate, the pump chilled faster than predicted.
NASA分類FACILITIES, RESEARCH, AND SUPPORT
レポートNO73N24278
N8110R:72-033
NASA-CR-132212
権利No Copyright
URIhttps://repository.exst.jaxa.jp/dspace/handle/a-is/199109


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