タイトル | Analysis of the STS-126 Flow Control Valve Structural-Acoustic Coupling Failure |
本文(外部サイト) | http://hdl.handle.net/2060/20100022153 |
著者(英) | McNelis, Mark E.; Jones, Trevor M.; Larko, Jeffrey M. |
著者所属(英) | NASA Glenn Research Center |
発行日 | 2010-05-01 |
言語 | eng |
内容記述 | During the Space Transportation System mission STS-126, one of the main engine's flow control valves incurred an unexpected failure. A section of the valve broke off during liftoff. It is theorized that an acoustic mode of the flowing fuel, coupled with a structural mode of the valve, causing a high cycle fatigue failure. This report documents the analysis efforts conducted in an attempt to verify this theory. Hand calculations, computational fluid dynamics, and finite element methods are all implemented and analyses are performed using steady-state methods in addition to transient analysis methods. The conclusion of the analyses is that there is a critical acoustic mode that aligns with a structural mode of the valve |
NASA分類 | Space Transportation and Safety |
レポートNO | E-17276 NASA/TM-2010-216339 |
権利 | No Copyright |
URI | https://repository.exst.jaxa.jp/dspace/handle/a-is/251373 |