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タイトルEvaluation of GLAS Demonstration Model Loop Heat Pipe Thermal Vacuum Performance with Various Fluid Charges
著者(英)Paquin, Krista C.; Grob, Eric; Butler, Dan; Swanson, Ted; Nikitkin, Michael; Baker, Charles; Ku, Jentung
著者所属(英)NASA Goddard Space Flight Center
発行日2001-01-01
言語eng
内容記述Two loop heat pipes (LHPs) are to be used for tight thermal control of the Geoscience Laser Altimeter System (GLAS) instrument, planned for flight in late 2001. The LHPs are charged with Propylene as a working fluid. One LHP will be used to transport 110 W from a laser a radiator, the other will transport 190 W from electronic boxes to a separate radiator. The application includes a large amount of thermal mass in each LHP system and low initial startup powers. This along with some non-ideal flight design compromises, such as a less than ideal charge level for this design concept with a symmetrical secondary wick, lead to inadequate performance of the flight LHPs during the flight thermal vacuum test in October of 2000. This presentation focuses on identifying; the sources of the flight test difficulties by modifying the charge and test setup of the successfully tested Development Model Loop Heat Pipe (DM LHP). While very similar to the flight design, the DM L14P did have several significant difference in design and method of testing. These differences were evaluated for affect on performance by conforming the DM LHP to look more like the flight units. The major difference that was evaluated was the relative fill level of the working fluid within the concentrically design LHP compensation chamber. Other differences were also assessed through performance testing including starter heater size and "hot biasing" of major interior components. Performance was assessed with respect to startup, low power operation, conductance, and control heater power. The results of the testing showed that performance improves as initial charge increases, and when the starter heater is made smaller. The "hot biasing" of the major components did not appear to have a detrimental effect. As a result of test results of the DM LHP, modifications are being made to the flight units to increase the fluid charge and increase the watt-density of the starter heater.
NASA分類Fluid Mechanics and Thermodynamics
権利No Copyright


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