タイトル | Assessment of inflow control structure effectiveness and design system development |
著者(英) | Peracchio, A. A. |
著者所属(英) | Pratt and Whitney Aircraft Group |
発行日 | 1981-10-01 |
言語 | eng |
内容記述 | Inflow control structures used during static testing of fans are shown to minimize inflow distortions and thus stimulate the inflight flow field and noise generating mechanisms. Acoustic tests are conducted on a Pratt and Whitney aircraft JT9D engine with and without an inflow control structure. Raw data are corrected to 77 deg, and time is averaged over 0.5 second intervals. Use of an inflow control structure is found to significantly reduce blade passage frequency tone, while having little effect on twice blade passage frequency tones, and significantly improves agreement between static data projected to flight and flight data for the blade passage frequency fan tone. A design system is also presented, which prescribes structure shape, size and construction. |
NASA分類 | AIRCRAFT DESIGN, TESTING AND PERFORMANCE |
レポートNO | 81A48637 AIAA PAPER 81-2048 |
権利 | Copyright |
URI | https://repository.exst.jaxa.jp/dspace/handle/a-is/414958 |
|